Road Trip!!

Tomorrow, I leave with the Boss body, hood, trunk and doors for Whitby Motorcars in Greensboro, NC.  If you click on the Customers button, there’s about 5 pages of cars that they’ve done in many different stages. They will go from the simplest small job to body work, paint & return to complete builds of Factory 5’s.

Whitby’s is going to have the body for a while. If they send me pics, I will certainly post them up here. In the meantime, say bye-bye….

Uber thanks to my old friend Bo for helping me get the body buck and the body into the trailer, and to another awesome friend Chip for the loan of the trailer. I couldn’t do this without you guys.

[edit]: So yes, I’m farming out the bodywork and paint. I’m a very good mechanic, but that doesn’t mean I can do anything. I know my limitations, Without the knowledge and experience, there’s no way I would have the patience to do this work. I’ve been told these bodies need at least 80 hours of work to be ready for paint, and I would end up with something crooked with lots of fisheyes and sanding marks. I know when to pay the pros. 😉

Peace-Out.

Working the hinges….

Started assembling my hood and trunk hinges today. The Roadster has an unusual hood hinge in that it’s a 4 link arrangement, allowing the hood to lift and then tuck in, to prevent the front edge from digging into the body.

Once I started putting all the pieces together (I had all the steel powdercoated last year), something struck me as not so cool.  There’s lots of side-to-side and front-to-rear alignment adjustment, but then there’s these wavy washers designed to go in between the bolted hinge points. When everything is bolted down tight on the shouldered bolts, it has a lot of flex and slop in the hinge assembly.

I may be proven wrong when everything gets assembled, but I didn’t like this. I also didn’t like that the wave washer is right up against my powdercoat, which could wear over time and then the steel starts rusting.

The copper-looking thing in the middle is an oilite bushing installed in the hinge arm.

If I removed the wave washers, with the nut tightened down to the shoulder bolt, that left a ton of room and made things even worse. Off to ACE Hardware for some washers. The idea is to use washers to take up the space so that the nut is tightening on the last washer and clamping everything together.

Here’s a comparison of what I did. The bottom assembly is with the wave washer and the top is without, but with a washer added to eat up the space. This worked wonderfully. I am able to use the nylock nut to fully tighten the hinge (tightening on the bolt threads and not on the shoulder), then back it off about 1/16 turn so that the assembly moves smoothly but with little to no slop.

Here’s the hinge installed and ready for the hood. The top bracket gets riveted to the hood. The 2 carriage bolts at the bottom are adjustable for side-side and fore-aft. There’s another pair of carriage bolts underneath to adjust height. In the background you can see the drivers side hinge laying flat.

Another update this evening as I’m on vacation and getting some work done… as well as a big update coming soon.

Headlights

I am on vacation later in January, so im taking the opportunity to move the Boss 427 body, doors, trunk lid, hood and hood scoop down to Whitby’s Motorcars down in Greensboro, NC. They are a premier Factory 5 body and paint facility. They also provide any level of assembly or finishing that you need. I will be getting all body work and paint done by them. I know it takes a lot of work, and I don’t have the patience nor the skill or experience for the level that I want on this car. A man has to know his limitations…

To prep for taking the body down south, I need to do a few things, one of which is to premount the exterior lights. I started with the headlights.

Time for more mods, right? Since the car is going complete LED lighting, I chose Watson’s Streetworx 7″ LED headlight system. This will replace the sealed beam halogen as supplied by Factory 5.

As I was putting these together, I was confounded by these little clips that hold the lamp to the adjustment ring. I assembled it as it should be with the screws and clips secure but not clamped down.

Next day when I got up, 2 of the clips had broken. Just from sitting overnight on the table. Can’t imagine what would have happened when installed in a rumpity rump car.

Since the LED kit uses a lens housing and a replaceable H4 style lamp, after much thinking and posting on the forum, I decided to glue / seal the lens housing to the adjustment ring. I would then make some small tabs out of aluminum and use standard #6 hardware to attach it all together.

 

Another item is that my new LEDs have 3 parts, all hardwired together. The LED unit, an LED driver and a plug. My plan was to mount the driver outside the bucket for cooling, but I’d have to drill about a 2″ hole to fit it through the bucket. Instead, I cut a slit from the lip of the bucket to where I drilled a 1/2″ hole for the wore and grommet. This way I was able to slip the wire through the slit, work the grommet into place and secure the slit. Now the lamp is inside while the driver is outside.

I will post up some.more pics when the units are assembled and on the car.

 

Continue reading “Headlights”

Overflow tank

In the forums, it’s been discovered that the coolant overflow tank is too small for almost any engine larger than a 302. Since mine is significantly larger… More mods!!

I bought a Canton tank from Summit that looked like it would fit well. There’s not much space left in the engine compartment, so I decided to mount it to the front X member. Since the mounts would never line up, I made an aluminum plate to secure to the X member with 2″ Adel clamps. Then I would bolt the coolant overflow tank to the plate.

This worked well. It left enough room to get the hoses to the fittings and fits right between the battery box and the power steering.

Locked it in place, ran the hose from the pressure cap and an overflow hose to the ground and filled it up. I’ll be running it to check a few things one weekend soon… This will be one of the things to check.

Getting pretty busy in the engine compartment….

Steering wheel

In the few times I’ve been sitting in the car, I’ve confirmed exactly what I always suspected…. It’s beyond small. Im a pretty big guy, so to help, I decided to install a quick release steering wheel.

I don’t have a lot of pics. It involved buying a kit from Breeze Automotive (Mark makes so many wonderful parts for this car). It requires welding a spline to the end of the steering shaft and them modifying the wheel mount.

The wheel mount is a beautiful piece of billet aluminum that Mark has custom made for us. It bolts to the QD on one side and the steering wheel on the other. To make sure it mounts to your wheel, you get to drill and tap it. 😁

Once installed, the wheel is secure with a bit of looseness. Im happy with bit for giving me increased access as well as a small level of additional security. I will update this post with another pic or two when able.

More seat work

You know I got the seat heaters installed, but at this point the heater wires were just hanging out of the side belt holes. More work to do.

I drilled a 1″ hole in the back inner corner of the seat for the wiring to come out. Had to get special grommets because of the 1/8″ thickness of the aluminum. I then installed the seat heater switches in the trans tunnel cover and used some Adel clamps to attach the wiring bundle with the relay to the back of the seat.

After this, I was able to get the seat mounts installed, set the seats in place and installed the seat belts. I was finally able to actually sit in my car!!

Since the pic was taken, I used a very sharp, new single edged razor blade to cut the threads and remove the badges from the belts. Looks much better. I am using RCI Platinum series 6 point harnesses, modified to 5 point. I chose to use these over the factory supplied Simpson harnesses simply because of the color and that the RCI’s use a camloc latching system. I like it.

Seats are set in place, belts are bolted in, adjusted and secure and the seat heaters are installed and working. Getting closer to playing go-cart….

Trunk work

Hey everyone,

Sorry for being gone for so long. Not only has the weather prevented me from having much garage time, my desktop computer crashed and it’s been a long process to get it fixed. I still haven’t accomplished that goal, so im trying to post updates from my phone. We’ll see how this goes.

 

One thing I have worked on is carpeting the trunk. Im using a grey almost felt-like material, similar to what you’d see on some speaker boxes. Cutting out pieces, gluing them in and keeping it looking good was a tough process. I would call the end result acceptable… Def not perfect and beautiful.

 

I also finished the area of what I call the glovebox or cubby… The area behind the rear bulkhead, accessible from between the seats.

 

Some seat work

Decided to do some seat work today. Its not out in the garage… I did with my dogs help in front of the TV. She mostly watched, but still…

These showed up from the UPS man the other day.

They are Kirkey model 47 Intermediate Road Race Seats. I got the 17″ wide version, which fits me quite well. The belts are RCI Platinum Series Kam-Lok 3″ racing harness’s.

First thing I did was cut the Kirkey label off the seats. They are rubber and I dont feel like doing all that advertising if I’m not getting paid. Then it’s time to install some seat heaters!

I’m installing Cobraheat waterproof seat heaters from Mike Forte at https://www.fortefactoryfive.com/. He’s a great supporter of this industry and sells a quality product.

Some guys had stripped the padding out of their seats to install the heaters right up against the fabric. I wasnt crazy about that and wasn’t sure I could put it all back together correctly. So I decided to install the heaters against the seat frame, but insulate it to project the heat into the seat. After researching some insulation type fabric stuff, I came up with some thermal batting called Insul-Bright., available right down the road at Jo-Ann Fabrics. Off I go and buy 1 sq yard for $7.99.

I cut this piece in half so it gave me a piece that 1.5′ wide by 3 feet long. Test fit it on the seat with a single piece of double sided aircraft carpet tape across the top.

Marked it, trimmed it,

taped the seat with more of the same tape,

…and stuck it all on there.

Next came the heaters.  The back, or upper, heater I decided to install full length. The lower heater wouldn’t fit, so I cut and trimmed it to fit. This is no problem with the elements as long as you are cutting the length. If you try to cut the width, you’ll cut off the power strips inside and then you’ll be cold. These I opted to spray glue onto the insulating batting because I felt the tape on the batting could end up doing something weird when it gets hot and maybe shifting.

So hopefully this will prevent the aluminum seats from becoming big heatsinks and soaking up all my seat heat when I need it the most. I’ve heard from other owners that it still works well and actually works to radiate the heat through all the padding.

Snapped the covers back on and snatched a pic real quick. Tomorrow I’ll get them wired up and see if they work…

By the way, sat in one and watched a movie this evening. They are pretty comfy… cant wait to drive in em. 🙂

 

details… and a parking brake

Hey Guys. Been working on a few small things, trying to wrap up some of the details before i move on to big items. Had a leaking lower radiator hose at the radiator, replaced a 3/4″ heater hose from Auto Zone that had a full length disbond in the hose. Cut that tab off the back of the frame and patched it. Finished drilling my Breeze stainless roll bars and bolting them in.

One thing I’ve put off because I didnt know how I was going to do it is the parking brake. Now this should have been done a long time ago.

I powdercoated and put together the F5 parking brake as supplied in the complete kit. I wasnt crazy about the location, and with it installed, it was too tight on the trans tunnel. The cables wouldn’t pull evenly and didnt really match up with the Wilwood calipers quite right. I decided to go with the Lokar EHB-7000F Universal Floor mount handle and the Wilwoods 330-10993 Universal E-Brake Cables for CPB calipers. The Wilwood cables include a cable equalizer for 2 cables, an adjustable cable housing mount and several tight fitting cushioned Adel clamps.

I removed the 4 angles from the Lokar and the Lokar clevis. Installed the Wilwood equalizer and installed the handle as far aft as I could on the RH side of the trans tunnel. I quickly saw that was a mistake, as there was nowhere to mount the Wilwood cable housing mount. So I moved it forward, using the original front bolt hole as the aft. I mounted it with some 3/8″ countersink bolts I had around and some .250 steel spacers to give the clevis room from the frame.

Since everything in there is at an angle, it became a challenge to mount the cable housing mount. Needed to keep it pretty straight with the handle. I decided to pickup the lower bolt mount through one of the diagonal supports and the upper would just mount to the aluminum using a 1″ steel spacer. I may go back and install a thick mounting plate that will bolt to the diagonal that will give more support to the cable mount.

Attached the Wilwood cables to the brakes, easy peasy, ran them around over the axle to the cable mount. Clamped in a few places. Pulled out the inner cables and cut the housings using a pair of heavy cable cutters. No issues. Installed the inner cables, ran everything up to the handle and locked em down. Cut the cables with a dremel cutoff wheel and duct taped the ends.

Used the adjustable equalizer to tighten up the cables quite easily. First pull, brakes are locked tight at the 3rd click. Easy to pull when seated and doesnt look too bad.

Also cut off the original bracket and patched the trans tunnel hole.

I know I may have an issue with leather boots and trim rings when I finish off the trans cover, but I have something of a plan for that that I hope will look pretty cool.

OK, on to more little stuff…

Big Weekend!

So over the last 2 days, I filled the transmission with 3 qts of Royal Purple Synchromax, filled the rear axle with 2 qts Royal Purple Max Gear (both synthetic), torqued on the wheels and got her off the dollies, charged the battery, bolted on the sidepipes, filled the cooling system with just distilled water (for now… leak checks), manually checked the clutch engagement and finally put 5 gallons of premium in it…

Then this happened.

It’s freeking alive.

 

Few things have happened

I have fixed a small coolant leak at the heater select valve, and replaced the power steering pump with a unit that is setup and dyno’d for flow and pressure to match the Fox Mustang steering rack. Also has a reservoir mounted right to the side of the pump for excellent fluid supply.

威而鋼的副作用

我治療背痛已經有20年了,我見過許多因為服用高劑量威而鋼後出現肌肉酸痛需要到醫院接受治療的陽痿患者,各種年齡和不同嚴重程度。

  • 壯陽藥的選擇技巧

樂威壯的效果

即使兩次服用的劑量合起來不超過20mg的安全劑量,大部分陽痿患者每次服用 樂威壯都會想到服用10毫克效果夠不夠?需不需要增加到20毫克?吃最大劑量會不會損害人體健康?