Cooling system

Worked on installing the radiator and hoses.

Factory 5 normally has you bolting the upper radiator to the frame, then the lower section is supported after the body goes on. I felt I needed something a little different. Another shopping trip to Breeze and I got upper and lower radiator mounts as well as some very cool upper and lower hoses. Also got a full coverage aluminum fan shroud.

When my brother was in town and we installed the engine a few weeks ago, he also started on the cooling system by mounting the fan to the shroud. That made my work shorter when I mounted the whole thing to the radiator. Then the upper and lower mounts are installed and voila… radiator is in.

Installed the upper and lower hoses. These are just plain cool. They are computer bent and beaded steel tubes, then powdercoated with silver ceramic inside and out. A short length of hose connects at each end.

small successes…

It’s been a while since my last update. A big item I’ve worked on has been the interior lighting. Factory 5 supplies a small 1 foot led strip light. If you want to split it up and use it in several places, you can cut it and solder on some new wires. Soooooo… that plan didnt work. I’m pretty good with soldering, but I could not for the life of me make those cut strip lights work. I had also planned on adding more lights.

So I went to Superbrightleds.com and did some searching. I bought 2 wired mini switches that were rated at 10 amps ($.95 each), 4 of the 6-led pod lights that self stick ($4.95 each) and a 40″ long led strip light that’s sealed ($18). Cool stuff.

Wired up the 2 footwells with 2 of the pods, using the headlight switch courtesy light function to control.

I then ran power wires from the same fuse to the Breeze Glovebox (remember my glovebox is behind the seats with a door in between) and the trunk. I wired in the mini switches with 2 light pods in the glovebox…

and the light strip in the trunk.

I know you can see the reflection of the individual leds in the trunk, but once the carpet goes in, you wont see that anymore.

Took a while to work out the wire routing and make it work, but I’m happy with the end result. It really looks better in person.

Electrical frustrations…

I’ve been working for close to 2 weeks on the pushbutton start / ignition system with RFID security. I’m not mentioning the companies name because I dont think it was an issue with them. They gave me good support and I believe they make a good product. I just dont believe their product is designed to work well with my setup.

So I gave up. I tried so many different ways, but every time I overcame one issue, something else wasn’t working as designed. And I mean the problems changed… one time the RFID wouldn’t program but the starter did kick in. When I fixed the RFID, then the starter would only engage when releasing the button. It just went on and on and I finally gave up. In 15 minutes, I removed the pushbutton start / RFID and had the Factory 5 keyed ignition installed and everything working.

With the keyed ignition, the Boss 427 finally gets to turn over! (Sorry about the noise in the video… had the big shop fan running)

And finally, my custom made gauges from Speedhut arrived. I designed everything about these… the font, the tick styles, the needles, the colors. The speedo is GPS driven. Although its a totally modern setup, yes the speedo operates backwards just like the original AC Ace and the Shelby Cobra.

History on the backwards speedo goes back to the AC Ace, the car that the Cobra was created from. Rumour is that when originally designing and building the car, the mechanical cable that ran from the transmission to the speedo was turning “anti-clockwise”. Normally, this would be fixed by a small gearbox on the back of the speedo. But AC decided to not add additional parts and simply operate the speedo backwards. When AC lost their engine contract and Carroll Shelby approached them with the idea of placing a Ford small block V8 in their car, he opted to leave it as is because he thought it was cool.

While I’m not building an exact replica by any means, I am proud to pay respect to the original in several ways. This is one.

And just as a side note, the 427 Cobra soon became the fastest production car in the world, capable of 0-100 and back to zero in less than 10 seconds. Backwards speedo or not. 🙂

Thanks for following…

Engine work…

Worked for a week on the engine front accessories. I’m running a 1-wire alternator, standard rotation Ford Racing water pump and power steering. After lots of research and looking, I decided on a setup from Jones Machine Racing Products. They make everything in house, including their power steering pumps and alternators.  After buying their kit for a small block Ford, of course I ran up against a few potholes. First, the power steering pump with integrated reservoir would not install… hits the steering shaft hard. So had to trade in for a slightly different pump with a remote reservoir. This means I also had to buy the material to make a -10AN supply hose.

Installing the crankshaft and water pump pullies was no issue. But did find that since the small block Ford kit is designed for a 302 and not a 351 based engine, ahem, the deck height is different and required a new, longer belt. Jones got me the right belt (with a spare!) and accepted the trade of my kit belts.

Now to install the alternator… looks like the kit is setup for a different standard rotation waterpump as some of the standoffs are not right. Quick call to Jones and they got the proper parts coming to me right away. One more quick hacksaw adjustment to the standoff behind the alternator to line up the pullies and voila… we have accessories!

Tomorrow I’ll finish up the heavy electrical and see if the car accepts power. Heard my custom gauge set from Speedhut is on its way…

Here’s another gratuitous picture of my girl because, hey, it’s my blog!

and the perfect way to finish up the day.

Cheers.

New Update!

Difficult to show electrical work, which is most of what I’ve been doing. Brother Bwana came up for a long weekend and even though I was battling sickness, I took advantage of the help to get the engine and transmission in. Just FYI, here’s some details: You know the engine (Ford crate Boss 427W). Parts I had to order and add: Ford billet steel zero balance flywheel, McLeod Super Street Pro clutch, all ARP bolts, Quick Time bellhousing and a Tremec TKO600 5 speed transmission with the cruiser overdrive.

So we got the engine in and secured. Bwana headed back to Asheville and I went into a medicated coma for about a week.

Get back to work! Still doing electrical. Started installing something cool that I’m adding… a Watson’s Street Works Hot Dot keyless ignition and RFID security system.

Took about 2 days to get it all wired in… and it wont turn on. Lots of troubleshooting later and I’ve done everything right. Both the RFID and the ignition will come on, but then cut right out again. Hint: I dont have a battery hooked up yet, so was using a 6amp 12v battery charger…

After talking to the head engineer at Watson’s, we figured the issue was the power source I was using. He suggested getting a good charged battery installed and properly wired and then try it. I tend to agree.

So lets do some battery! Not a lot to show, except I’m custom building every cable. 4ga from battery + to start solenoid, 4ga from battery – to chassis ground, 4ga from chassis ground to engine block. Also a 10ga from the alternator + to a cutoff switch and then to the battery +, and a 10ga negative cable from the alternator case to the engine block.

Still have some small details to finish up, but will be slapping some battery power to the Boss tomorrow! Hope I dont let all the smoke out…

 

The powerplant is in!

Guest Blog Entry By Bwana

Sunday’s goal was getting the engine and transmission assembly shoe horned into the frame and mounted.

That’s a serious load of engine for this tiny frame

(sorry about the crappy exposure)
Move an inch, change the angle, check clearances, move an inch, …
It fits!

Engine & Transmission Assembly

By Bwana

Hey Everyone,

I came up from Asheville for a long weekend to work with Boyd on The Boss. We spent two days of full-on work. Saturday was spent assembling the transmission to the engine and all that that entails.

A healthy flywheel mounts to the end of the engine crankshaft, then there’s a clutch, pressure plate, bell housing, assorted clutch actuators, then the transmission.

Boss 427 Clutch
Pressure Plate (not yet installed)

One item held us up significantly: three small pins that align the pressure plate to the flywheel. We did not have these and could not go any further without them. Luckily, we found them at a local Ford dealer. We had to wait several hours, but the dealer came through and we got back to work.

This little pin (three total) cost us a few hours

The tough bell housing is installed, ready for the transmission
Boss 427 Engine & Transmission Assembly

Big Weekend…

Been keeping busy on the Boss, just not doing stuff that’s very photogenic.  Lots of wiring up switches and running harness’s mostly. Started working on the footbox fans and will update you on that later, but for now…

My brother Bwana came up from Asheville for a long weekend and we decided it was time to do some major stuff.  He got to dig in and turn some wrenches on The Boss, so I’m going to let him do a Guest Blogger Entry and post his own pics and update. Keep watching… but here’s a teaser

Some good steps forward

So the engine I bought has an oil pan that hangs too low. It would hang about 3/4″ below the frame rails… not good for ground clearance. I bought a new pan and pickup from Breeze and worked on installing that this week.

Inside the Boss427. Pure Art.

When I replaced the oil pickup, we had an immediate clearance problem.

The rod for #3 cylinder hits the oil pickup tube. Installed a 1/4″ stack of washers under the bracket and voila!

We now have clearance. If that rod had been allowed to wear a hole in the tube, the oil pump would have been drawing air instead of oil and the engine would have lost oil pressure. This could result in either a major inconvenience… or total engine destruction. Its good now!

Spent the better part of 2 days getting the headers to fit. Some of the bolt holes were not lining up very well at all. A total of 6 (out of 16) bolt holes had to elongated, and this stainless is tough stuff. Finally got the headers on for a good fit. Final install will be after the engine is installed.

Worked on my glove box. This has been a thorn in my side trying to find the right concealed hinges to make this work. I finally decided a stainless piano hinge would not look too bad and could be easily worked into the plan. So got that cut and installed today. Its only temporary until I start doing leather and carpet. It will have some reinforcement to stiffen the door and also a locking latch out of a 70’s era VW bug.

Lastly, some cool stuff showed up today. You’ll see these within the next week or so…

Hope everyone is having a good week!

First color

Ok, really short post. Excited to say I ordered the first item that involves color choice today. Placed an order for the leather that will cover the dash, center console, rear glove box door, shift and brake boots and possibly the rear bulkhead. Purchased from The Leather Hide Store.

Also a tip to the external colors I’m working on. This will be very close to the stripe color, although that paint will be in metallic.

Yowza. Aint that nice?

Few things have happened

I have fixed a small coolant leak at the heater select valve, and replaced the power steering pump with a unit that is setup and dyno’d for flow and pressure to match the Fox Mustang steering rack. Also has a reservoir mounted right to the side of the pump for excellent fluid supply.

威而鋼的副作用

我治療背痛已經有20年了,我見過許多因為服用高劑量威而鋼後出現肌肉酸痛需要到醫院接受治療的陽痿患者,各種年齡和不同嚴重程度。

  • 壯陽藥的選擇技巧

樂威壯的效果

即使兩次服用的劑量合起來不超過20mg的安全劑量,大部分陽痿患者每次服用 樂威壯都會想到服用10毫克效果夠不夠?需不需要增加到20毫克?吃最大劑量會不會損害人體健康?